Couldn't hold the nut Max, so it got JB Weld so see how that goes. Strange thing though the tank had about half a litre of what looed and smelt like old engine oil in it. Glad I pulled the tank off to seal up the nut and I was able to get all that gunk out of it.I certainly would prefer not to have to make up these weights for these PT's but I see in the future F/C's might be hard to get and all we have left is PT's to fit on these slashers so I put the hours I have spent on it as research for the future
Anyway just an update the PT motor on a 24 is an excellent motor but it requires the extra weight on the crank. This one makes not the slightest attempt to kickback and it is running a decomp valve with no restrictor in it. Next time I will try one with half the weight in it, I will make the pipe 18mm long and fill that with lead and see how close it gets to kicking back. It is all trial and error to get it right

Last edited by NormK; 30/12/22 04:41 PM.